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Leo Glenn Murry

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Leo Glenn Murry

Birth
Kansas, USA
Death
27 Apr 1953 (aged 42)
Sweetwater County, Wyoming, USA
Burial
Rawlins, Carbon County, Wyoming, USA GPS-Latitude: 41.7974987, Longitude: -107.2400254
Plot
OSJ-C-7-3
Memorial ID
View Source
Killed in the tragic wreck of the 4005.

Leo Glenn Murry, 42

Murry was an employee of the Union Pacific Railroad for 20 years and an engineer at the time of his death.

He was survived by his wife Lillian and two children, Patricia, 13, and Michael, 9.

He was a member of the Fraternal Order of Eagles, Council 2128, Knights of Columbus, the Order of St. Christopher for Catholic Railroadmen, Junior Old Timers, and the Brotherhood of Fireman and Engineers.
_____________________________________

On April 27, 1953 the crew of the Union Pacific 4005 freight train started out on a routine haul across the open prairie of southern Wyoming. Engineer Leo Murry, Fireman Lawrence (Ed) Endres, and Brakeman James R. Anderton made up the head end crew. Conductor James Walker and Brakeman Ivan Shurigar made up the rear end crew. Sixty-two cars and a caboose followed the giant 600-ton ‘Big Boy’ locomotive and it lumbered along the tracks.

At 9:10 a.m. the train passed through Wamsutter, Wyoming, headed westbound not knowing that in just 10 minutes the unthinkable would happen. The morning was cloudy with a light mist and the 0.43 percent descending grade made for easy travel. All seemed normal.

At this same time just 8.5 miles to the west another event was unfolding. A section gang stationed at Frewen traveled 3.6 miles to the east to Red Desert on a track motorcar to obtain a supply of switch ties. The foreman and four section workers arrived in Red Desert and were approached by a sheep herder requesting assistance in getting his sheep across the tracks. (The size of the sheep herder’s herd is not known, however, the average ranch in 1949 had 1,100 head of sheep). The foreman called to receive a track line-up which read, “Westbound, Extra 4005 West, Red Desert 9:15 a.m. Westbound, Extra 1480 West, Red Desert 9:50 a.m. Eastbound, Extra 3969 East, Red Desert 9:15 a.m. Eastbound, Extra 1470 East, Red Desert 9:55 a.m.”

After he received the line-up information the foreman assigned one section man to proceed eastward and other westward to provide flag protection at each end of the side track. After one eastbound and one westbound train passed they were to provide protection for the sheep herder. As added protection, two other section men were to open a switch in each main track, which led to the siding. This would display a block signal down the track in each direction warning any unannounced approaching trains to slow down. The foreman unlocked both switches and the section men were instructed to open the switch on his hand signal. The foreman then walked back to the sheep herder, some 300 yards from the switch, to tell him what the men were going to do.

As the 4005 approached the east end of the Red Desert siding the Union Pacific section man opened the siding switch and then, seeing the massive locomotive barreling downon him, frantically made an unsuccessful attempt to close it before the engine passed. The engineer made an emergency application of the brakes as the engine entered the siding.

The 4005 entered the open switch at 50 mph causing it to careen off the rails and skid along its left side tearing up rail and roadbed. The locomotive, tender, and first 18 cars derailed. The cab of the locomotive was destroyed as the tender tore into it twisting and smashing the metal. The first 12 cars were badly damaged and piled in a 70' high heap. The thirteenth to the seventeenth cars were somewhat damaged from the force of impacting against each other and toppling off the rail. Scattered about the scene was the train’s load: tractors, dead hogs, typewriters, sewing machines, and other merchandise.

The engineer Leo Murry and fireman Lawrence Endres were killed instantly, and amazingly the front brakeman, James Anderton, was alive.

The rear crew did not know anything was wrong until they saw the emergency signal from the engineer. When they looked out and saw the cars piling they both rushed out of the caboose. Walker headed to the front of the train and using a dispatchers phone called in what had happened. He could not get near the wreck, as the hissing steam billowed around the injured train. It took nearly 25 minutes for the steam to subside.

Shurigar protected the rear of the train by walking a mile back east to set two torpedoes on the track so that the engineer of an oncoming train would be warned and not collide into the back of the derailed train.

Brakeman Anderton’s left leg was twisted and pinned between a wooden seat and the steel side of the cab. He was trapped in an area of the cab no larger than 18” high and four feet wide for ten hours while rescue workers removed tons of coal and cut through steel to free him. Anderton asked rescuers for a drink of water and a cigarette. A doctor was able to reach into a narrow opening and administer a dose of morphine to subside Anderton's terrible pain. Anderton later told rescuers that his hands hurt and that he was “chilling a little” but could no longer feel pain in his foot.

Anderton also told a rescue worker, “He threw it right in front of us. The switch, they threw it right in front of us, they didn’t give us a chance. I felt the engine rock. I don’t know how many times it rocked. The next thing I knew I felt the steam hitting me in the face and I thought I was a goner. All I could think of was getting my hands over my face.” Anderton died at 10:57 a.m. on Wednesday, April 29, from second and third degree burns covering 80 per cent of his body, severe prolonged shock, and other complications.

Early reports indicated that the engineer and fireman were alive after the accident, as two workers said they spoke to the men. This later turned out to be false; the two workers were actually talking to each other from opposite sides of the train.

Track crews worked swiftly to clear the wreckage. East and west rail traffic was delayed for nine hours until the construction crew could install a shoofly to route rail traffic around the accident site. Priority was to resume a normal traffic schedule. Some westbound trains were re-routed through Cheyenne on the Denver and Rio Grande.

Many of the four car loads of pigs were killed upon impact. According to workmen at the site some pigs provided comic relief during the emotionally and physically draining rescue operation. Occasionally a pig would regain consciousness and with a terrific grunt would take off running through curious bystanders.

Anderton, before he died, provided some key information in determining exactly how the accident happened and who was at fault. Anderton noted that he and Endres had seen a man throw the switch and yelled to the engineer. Murry ran across the cab, looked, and then ran back and ‘big-holed’ it. Big-holed was the term used to describe applying the emergency brakes.

During the investigation Puerto Rican section worker Ralph Vicenty, through an interpreter because he did not speak or understand much English, said the foreman had shown him how to operate the switch and when the foreman walked back to the sheep herder it was the foreman who left the switch in the open position. It was later determined that this could not have been the case because the open switch would have displayed a signal to the oncoming 4005 providing enough time to stop safely.

Union Pacific Railroad and Interstate Commerce Commission officials reached the conclusion that Kenneth M. Mayfield, foreman, and Ralph Vicenty, section worker who had been working with the UP for only one hour and twenty minutes, were responsible for the accident. There were considerable variances between their stories, each blaming the other. The Interstate Commerce Commission, Union Pacific Railroad, and local officials investigated the accident. A meeting closed to the public and press was held to determine how the accident occurred and who was responsible. The Sweetwater County coroner’s jury found Mayfield guilty of negligence for putting an irresponsible man in control of the switch. Section worker Vicenty was found responsible for throwing the switch onto a side track.

By 1962 all twenty-five of the ‘Big Boys’ were retired. Today eight of the original twenty-five are in museums across the nation. Visit the Forney Museum of Transportation at 4303 Brighton Blvd., Denver to see the Union Pacific 4005. Our 4005 was rebuilt by Union Pacific at its Cheyenne facility. It is possible a different tender was used in the rebuilding. The Big Boy shows very little evidence of the wreck damage today.

Information courtesy of Information courtesy of Deb Davidson, May 2015.
Killed in the tragic wreck of the 4005.

Leo Glenn Murry, 42

Murry was an employee of the Union Pacific Railroad for 20 years and an engineer at the time of his death.

He was survived by his wife Lillian and two children, Patricia, 13, and Michael, 9.

He was a member of the Fraternal Order of Eagles, Council 2128, Knights of Columbus, the Order of St. Christopher for Catholic Railroadmen, Junior Old Timers, and the Brotherhood of Fireman and Engineers.
_____________________________________

On April 27, 1953 the crew of the Union Pacific 4005 freight train started out on a routine haul across the open prairie of southern Wyoming. Engineer Leo Murry, Fireman Lawrence (Ed) Endres, and Brakeman James R. Anderton made up the head end crew. Conductor James Walker and Brakeman Ivan Shurigar made up the rear end crew. Sixty-two cars and a caboose followed the giant 600-ton ‘Big Boy’ locomotive and it lumbered along the tracks.

At 9:10 a.m. the train passed through Wamsutter, Wyoming, headed westbound not knowing that in just 10 minutes the unthinkable would happen. The morning was cloudy with a light mist and the 0.43 percent descending grade made for easy travel. All seemed normal.

At this same time just 8.5 miles to the west another event was unfolding. A section gang stationed at Frewen traveled 3.6 miles to the east to Red Desert on a track motorcar to obtain a supply of switch ties. The foreman and four section workers arrived in Red Desert and were approached by a sheep herder requesting assistance in getting his sheep across the tracks. (The size of the sheep herder’s herd is not known, however, the average ranch in 1949 had 1,100 head of sheep). The foreman called to receive a track line-up which read, “Westbound, Extra 4005 West, Red Desert 9:15 a.m. Westbound, Extra 1480 West, Red Desert 9:50 a.m. Eastbound, Extra 3969 East, Red Desert 9:15 a.m. Eastbound, Extra 1470 East, Red Desert 9:55 a.m.”

After he received the line-up information the foreman assigned one section man to proceed eastward and other westward to provide flag protection at each end of the side track. After one eastbound and one westbound train passed they were to provide protection for the sheep herder. As added protection, two other section men were to open a switch in each main track, which led to the siding. This would display a block signal down the track in each direction warning any unannounced approaching trains to slow down. The foreman unlocked both switches and the section men were instructed to open the switch on his hand signal. The foreman then walked back to the sheep herder, some 300 yards from the switch, to tell him what the men were going to do.

As the 4005 approached the east end of the Red Desert siding the Union Pacific section man opened the siding switch and then, seeing the massive locomotive barreling downon him, frantically made an unsuccessful attempt to close it before the engine passed. The engineer made an emergency application of the brakes as the engine entered the siding.

The 4005 entered the open switch at 50 mph causing it to careen off the rails and skid along its left side tearing up rail and roadbed. The locomotive, tender, and first 18 cars derailed. The cab of the locomotive was destroyed as the tender tore into it twisting and smashing the metal. The first 12 cars were badly damaged and piled in a 70' high heap. The thirteenth to the seventeenth cars were somewhat damaged from the force of impacting against each other and toppling off the rail. Scattered about the scene was the train’s load: tractors, dead hogs, typewriters, sewing machines, and other merchandise.

The engineer Leo Murry and fireman Lawrence Endres were killed instantly, and amazingly the front brakeman, James Anderton, was alive.

The rear crew did not know anything was wrong until they saw the emergency signal from the engineer. When they looked out and saw the cars piling they both rushed out of the caboose. Walker headed to the front of the train and using a dispatchers phone called in what had happened. He could not get near the wreck, as the hissing steam billowed around the injured train. It took nearly 25 minutes for the steam to subside.

Shurigar protected the rear of the train by walking a mile back east to set two torpedoes on the track so that the engineer of an oncoming train would be warned and not collide into the back of the derailed train.

Brakeman Anderton’s left leg was twisted and pinned between a wooden seat and the steel side of the cab. He was trapped in an area of the cab no larger than 18” high and four feet wide for ten hours while rescue workers removed tons of coal and cut through steel to free him. Anderton asked rescuers for a drink of water and a cigarette. A doctor was able to reach into a narrow opening and administer a dose of morphine to subside Anderton's terrible pain. Anderton later told rescuers that his hands hurt and that he was “chilling a little” but could no longer feel pain in his foot.

Anderton also told a rescue worker, “He threw it right in front of us. The switch, they threw it right in front of us, they didn’t give us a chance. I felt the engine rock. I don’t know how many times it rocked. The next thing I knew I felt the steam hitting me in the face and I thought I was a goner. All I could think of was getting my hands over my face.” Anderton died at 10:57 a.m. on Wednesday, April 29, from second and third degree burns covering 80 per cent of his body, severe prolonged shock, and other complications.

Early reports indicated that the engineer and fireman were alive after the accident, as two workers said they spoke to the men. This later turned out to be false; the two workers were actually talking to each other from opposite sides of the train.

Track crews worked swiftly to clear the wreckage. East and west rail traffic was delayed for nine hours until the construction crew could install a shoofly to route rail traffic around the accident site. Priority was to resume a normal traffic schedule. Some westbound trains were re-routed through Cheyenne on the Denver and Rio Grande.

Many of the four car loads of pigs were killed upon impact. According to workmen at the site some pigs provided comic relief during the emotionally and physically draining rescue operation. Occasionally a pig would regain consciousness and with a terrific grunt would take off running through curious bystanders.

Anderton, before he died, provided some key information in determining exactly how the accident happened and who was at fault. Anderton noted that he and Endres had seen a man throw the switch and yelled to the engineer. Murry ran across the cab, looked, and then ran back and ‘big-holed’ it. Big-holed was the term used to describe applying the emergency brakes.

During the investigation Puerto Rican section worker Ralph Vicenty, through an interpreter because he did not speak or understand much English, said the foreman had shown him how to operate the switch and when the foreman walked back to the sheep herder it was the foreman who left the switch in the open position. It was later determined that this could not have been the case because the open switch would have displayed a signal to the oncoming 4005 providing enough time to stop safely.

Union Pacific Railroad and Interstate Commerce Commission officials reached the conclusion that Kenneth M. Mayfield, foreman, and Ralph Vicenty, section worker who had been working with the UP for only one hour and twenty minutes, were responsible for the accident. There were considerable variances between their stories, each blaming the other. The Interstate Commerce Commission, Union Pacific Railroad, and local officials investigated the accident. A meeting closed to the public and press was held to determine how the accident occurred and who was responsible. The Sweetwater County coroner’s jury found Mayfield guilty of negligence for putting an irresponsible man in control of the switch. Section worker Vicenty was found responsible for throwing the switch onto a side track.

By 1962 all twenty-five of the ‘Big Boys’ were retired. Today eight of the original twenty-five are in museums across the nation. Visit the Forney Museum of Transportation at 4303 Brighton Blvd., Denver to see the Union Pacific 4005. Our 4005 was rebuilt by Union Pacific at its Cheyenne facility. It is possible a different tender was used in the rebuilding. The Big Boy shows very little evidence of the wreck damage today.

Information courtesy of Information courtesy of Deb Davidson, May 2015.


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